Improved Operation In CANDU Plants With CAN8 PHT Pump Seals

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T. Graham
D. McInnes
D. Rhodes

Abstract

The CANS PHT pump seal is currently operating in twenty-one pumps, twelve at Bruce A, seven at Bruce B and in both pumps at Grand Gulf Nuclear Station (GGNS). The CANS seal has markedly improved performance over the CAN2 seal previously used at the Bruce stations and the SU seals previously used at GGNS. Details of the performance improvements are discussed. Prior to installation in Bruce B, the CANS seal was slightly modified and then demonstrated to be resistant to reverse pressurization failures, since this was a known failure mechanism with the CAN2 seal. Subsequent experience showed that Bruce A was also susceptible to reverse pressure incidents. A review of plant operating procedures at Bruce A showed reverse pressure was likely the initiating factor for several previously unexplained seal disturbances. The reverse pressure failure mechanism is described, as are the improved system operating procedures designed to prevent it. Preventative procedures have now been implemented across Ontario Hydro Nuclear. The ability to track down seal failure mechanisms such as this is greatly enhanced by the improved system monitoring and data retrieval now in place at Bruce A and Bruce B.

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