Darlington Station Outage-A Maintenance Perspective
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Abstract
Ontario Hydro's Darlington Nuclear Generating Station (4x881 MW(e)net) has carried out its first station outage since full commercial operation. The outage presented challenges to the organization in terms of outage planning, support, management, and safe execution within the constraints of schedule, budget and resources. This paper will focus on the success of the outage maintenance program, identifying the major work programs -- a Vacuum Structure and Containment Outage, an Emergency Service Water System Outage, an Emergency Coolant Injection System Outage, Intake Channel Inspections, Low Pressure Service Water Inspections, and significant outage maintenance work on each of the four reactor units. Planning for the outage was initiated early in anticipation of this important milestone in the station's life. Detailed safety reviews -- nuclear, radiation, and conventional -- were conducted in support of the planned maintenance program. System lineup and work protection were provided by the Station Operator work group. Work protection permitry was initiated well in advance of the outage. Station maintenance staff resources were bolstered in support of the outage to ensure program execution could be maintained within the schedule. Training programs were in place to ensure that expectations were clear and that high standards would be maintained. Materials management issues in support of maintenance activities were given high priority to ensure no delays to the planned work. Station management review and monitoring in preparation for and during the outage ensured that staff priorities remained focused. Lessons learned from the outage execution are being formalized in maintenance procedures and outage management procedures, and shared with the nuclear community.
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